Shop Goin’ Ons Late Januaryn2020

Time for my bi-monthly shop update.

Screaming Woody

The new motor is in the Screamin’ Woody and I took it for a blast down my nasty rural road. Appears to be fine, but I didn’t take it above 4500 RPM as we’ve had a lot of rain and the 35mph road is pretty rough. Changed the preload a little to help it launch straighter – but haven’t test that. I’ll come to Bradenton a day early and try to work out the wrinkles.

Back at the shop I put it on the rack. Changed the breakin oil for racing oil, cleaned the underside, and found a crimp in the fuel line making a 90 degree turn – so it was cut out and replaced with a couple 45 degree hose ends and a m/m fitting. Polished the wheels, put it back on the ground to clean under the hood, interior and exterior.

She’s ready to go into the Stacker when I finish out-fitting it.

The Thug

Because the Screamin’ Woody will be untested before the race in Bradenton, FL in early March, I’m gonna throw the Thug on the Lift as a backup, in case there’s an issue with the Screamin’ Woody. So it too had its oil changed, wheels polished and a through detailing.

Tool Time with Jake

In the above photo, you see Grandson #2 – Jake. He and his twin sister Elwood spent a few days with Deb and I, as their mother was having a medical procedure. Jake spent a 1/2 day in the shop learning a little about tools and cars.

He naturally wanted to grab a seat (including back seat) in the three cars in Shop 1 – where most of the work is done. Afterwards, he learned how to mark a 1/2″ impact wrench holster level on the Stacker door, drill through one panel while stopping before going through the outside skin, and riveting the holster on the door.

As I was trying to show him how to mount and wire up a 9000# winch in the Stacker, I found that a 5-year-old boy’s 1st tool-time (keep in mind I have two sons and three handy daughters – so this isn’t my first rodeo) has limited patience. To get him to stop rummaging through the tool drawers in the Stacker, I used the “Ole Tape Measure Trick” and had him measure some stuff.

After he got bored of that, he decided Tool-Time was over and decided to play on the playground I built in front of my house a couple of years ago.

Stacker

So speaking of the new Stacker, I need to finish out-fitting it so I can load the cars up. Check a couple of previous posts to update yourself where I’d gotten by mid last month. Most is done, but the winch (to get the cars in and out of the trailer) was not.

When I ordered the Stacker built to what I’ve learned about trailers over the years, I had them build an in-floor compartment for a winch with 1/2″ platting. There’s a door that covers it to make for a flat floor. I test fitted the winch and drilled some 1/2″ holes through the plate. The winch was then mounted by bolting in from the under the trailer, using Grade 8 hardware.

Once bolted in, it became obvious that Intech didn’t make the well deep enough for the relay box that sits on top. I took it apart to remove the mount, and the only place it would fit was in back of the winch – only if I removed the lower mounting rod off the winch.

Even then, I only had about 1/2″ clearance from the now neatly rolled spool. Since we all know this will be the last time the spool will be neat – that wasn’t going to work. I removed the relay and rolled under the trailer with it and a mount I had made from aluminum bar stock. After tearing out a clump of hair caught in the creeper’s wheel, I remembered that now that my hair is again Long – that I have to have hoodie up when on a creeper.

I then drilled a 2″ hole through the 1/2″ plate, almost breaking my wrist many times when the broch stopped moving but my big Dewalt drill still wanted to turn.

It would only be Natural that after taking two shots of mounting the relay box under the trailer that the cables to the winch would all be 1″ too short. So work stopped on the winch while I placed an order for 4Ga copper cable butt connectors and a couple options on 2″ hole grommets.

However, there was other work to be done.

Like a couple door baskets, disposable glove holder, magnetic bars for wrenches, and a couple Velcro straps to hold a yoga mat for me to lay on when under the car.

Mounted power tools, batteries and charger on bench splash board, and an oil pan holder on the wall under the oil rack. I should have the Stacker finished and the cars loaded in by the end of next week.

The Old Aluminum Trailer

If you’ve been following along, you’ll know that I have a 25 year old aluminum trailer I’m making new again. A few posts back I showed how the inside and outside was stripped and painted, new LED tail and marker lights, reflective Red/White/Blue stripes, Texas Flag painted on door, and about half of the out-fitting done. Since then:

I cut a 1″ square 3/16″ steel plate into four 6″x6″ plates, punched 1/2″ holes in them, primed and painted White to match the trailer. They’ll be backing plates to the Puck lock, to spread the stress on the inside and outside of the door, inside and outside of the trailer. I’ll be mounting the Puck lock next week.

At the rear of the trailer I mounted a jack pouch, spare tire, and blower on the curb side. On the street side – I mounted a strap holder with a cut down yoga mat as a wall protector. A broom holder and a holder for my director’s chair – in the black bag. Also hung a couple cord holders. I mounted some small D-Rings for bungee cords – to keep stuff from flopping or falling onto my car – as this is a very narrow trailer. I also secured the basket holding the jacks with bungee cords and D-Rings. That’s for in case the car gets too close winching out and I need to get them out of the way. The plan is to be able to quickly get to the spare, two bottle jacks and tire spinner by just opening the rear door – and not having to climb over stuff. I have much experience with flats as I drive fast, for long periods of time, on hot southern roads.

Moving to the front curbside of the trailer, I have a door cabinet with drop down table top, wrench/oil rack, fire bottle holder and a disposable glove holder on the door. On the side of the cabinet, I have rubber hands to hold the Weather station pole that extends above the trailer. Outside the door I have a White Board to leave and receive messages when I’m not in my pit. Inside next to the door is a strap rack with a yoga mat protector.

On the front street side:

I have hangers for my power tools, racks for papers and my log book, double helmet rack with stereo under and speakers to the side, a couple magnetic bars and some hand tools mounted. I still have to wire in two batteries, an inverter, a charger, the roof fan, the stereo, a pair of charging lugs and other incidentals. I also need a cover for the radio and plumb for compressed air receptacles under door and rear of trailer.

The Petty Tribute

The gas sending unit in tank was swapped so the gas gauge now works. The shifter was hitting the steering wheel in 1st and second, so a spacer was made to fix that. The retro tach still doesn’t work, so I need to deal with that. The car was cleaned up.

I dug up three old 15″ Mopar wheels for the front, and spare. I took them down to Discount for my bud Gregg to dismount the rotted tires. They were cleaned up, prepped and I hit with rust colored primer. Next week I’ll play around with cream paint and primer to make look rusty like the back wheels and then take to Discount for some new Goodrich T/As to get mounted. Then the car is done.

Ginger, my Magnum XE

The Gear Vendors overdrive is in the car, just waiting for the Driveshaft from Victory. It arrived yesterday, and that car should be back on the road next week.

The Skipper – My Magnum GT

The engine and Transmission was pulled.

All of the under hood parts were pulled.

Under the hood will get cleaned, wire brushed and scuffed before receiving a fresh coat of urethane to match the exterior. The engine will cleaned resealed and painted – as will the transmission. Then gets stabbed back in. The AC compressor cleaned and painted. The wiring cleaned – maybe replaced if I can find new authentic. Power steering pump replaced, hard lines either made to look new or replaced. I want under the hood to look as new as the exterior.

So I think that catches me up on the shop reporting. Next report in about two weeks.

Old is New Again

The refurbishing of a early 90s aluminum race trailer

About 18 months ago, I bought an early 90s Aluminum Trailer from a racing buddy. The reason was that I had a Motorhome and a Stacker Trailer for week long races, a pick-up truck and gooseneck for weekend races, and a Toy Hauler and pick-up for motorcycle trips. The Toy Hauler needed to be replaced because it was shit and cost me money every time I took it out. I came up with brilliant money saving idea that buying an older, quality, aluminum trailer would allow me to sell both the Toy Hauler and Gooseneck. I could take the Motorhome and trailer (If I set up to carry both my son’s and my Harleys) on motorcycle trips and pull it behind the pick-up for weekend racing.

So I buy this early 90s trailer from Jim Bailey. I paid a premium for it, but it was well cared for and I felt I could freshen up reasonably. To this date, I modified the interior floor to accept the “Lock ‘N Loads to transport bikes, added a winch, some D-Rings, and move the wheel stops to accommodate a bigger car. I then scuffed, prepped and painted the exterior walls white with Red & Blue Stripe. It cost me a gallon of Rustoluem white and a quart each of red and blue Rustoleum – plus some supplies. I also painted the A-Frame gloss black. I later replaced the red and blue stripes with red, white and blue reflector tape – and wrapped the bottom in red/white safety tape. Electrically, I replaced all marker and tail lights with LED and the 7-blade trailer wiring. Finally, I installed an electric jack. Below are a list of shop update links on Maniacal Ravings of Dave Schultz, where I posted Details and Photos of this work.

So the above brings you up until this last week. Everything on the wall was removed and the interior walls were scuffed with 400 grit on a DA Sander, wiped down, taped off, and painted while with a roller.

Then I started to outfit to my convenience. I started with buying a black Yoga mat, cutting it in half, and riveting into place (with 1″ aluminum stock) at the back of the trailer. I then mounted a broom holder, strap holder, cord and hose holders and the Spare tire. I also mounted a hanger for the Director’s chair carrying case.

Moving to the front, I mounted a double helmet closet next to the bench. Onto it I installed a Kenwood stereo and a pair of speakers. To pick up the track radio from pitted in the Boonies, I mounted a high quality antenna on the street side – extending above the roof.

You’ll also note the 12,000 pound winch with a wireless remote mounted against the wall and a removable snatch pulley in the center. Also on the floor are the Lock ‘n Load plates for the removable motorcycle chocks.

Moving to the door, I mounted a door cabinet with fold down table. Below that is an oil bottle shelf, which also holds wrenches and screw drivers. That should alleviate some of the running in and out of the trailer for the most basic tools.

And speaking of convenience, I bought another cheap Yoga mat with carrying strap and riveted the sprap above the door. That makes it easy to grab for those times in the pits when you need to lay on the ground or work under the car.

I still need to:

  • Replace the trailer lights junction box with waterproof new
  • Mount dual batteries with cutoff switch under bench
  • Wire stereo and speakers
  • Wire roof exhaust fan
  • Run air lines under the trailer from rear and side door to air compressor under bench, and wire a on/off switch on bench
  • Make a rack for a set of 4 jack stands
  • Mount a rack for two bottle jacks and tire spinner under the spare
  • Mount a front strap holder and wall protection
  • Mount a 12V fan under upper cabinets
  • Mount a intelligent trickle charger for when the trailer is plugged in
  • Mount a set of Charging Lug on A-Frame to charge batteries
  • Install an inverter to provide AC power from a pair of DC batteries
  • Replace 4′ florescent ceiling lights with LED
  • Mount a LED pit light

Shop Goin’ Ons For December 2019

Petty Tribute

I aged some 15″X8″ Wheel Vintiques wheels to look Rusty, and mounted 245/60-15 Goodrich TAs on the rear. I still need to do the same for the fronts.

I repaired the old steering wheel, primed and painted to match the interior.

I tried three different shifter handles and all hit the seat, dash, or both. I finally made a 6″ adaptor to raise a pistol grip shifter 6″, which was enough to clear the bench seat and stay under the boot.

I bought all of the pipes needed to get the block hugger collectors to 2.5″ side exiting exhaust. This is all that is required to finish the car. These are the pipes needed to do the right side.

Magnum GT

If you’ve been following along on the Magnum GT, You’ll know it was recently treated to a new poly-urethene paint job, and the leather dyed before that. This week, everything was taken out of the trunk, the Surface flash removed, it was then masked, primed and painted. Since the car is pure black, it was an easy rattle can project. I’ll give the a paint a week to get hard, and then clean and replace the carpet.

The Screamin’ Woody

The engine was reassembled with a new crank, rod, and set of lifters; and stabbed into the car. It will be started and tuned next week.

Outfitting the Stacker

I spent a day getting the Stacker trailer mostly outfitted. On the door I installed a door cabinet fire bottle holder, tire gauge holder, rack of screw drivers and a pair of clamps that hold the weather station in travel mode, and the telescopic pole it goes on (to raise 5′ over the stacker’s roof) when in the pits. Another set of clamps were installed inside the door to hold the pole in travel mode.

On the front wall of the trailer, I mounted a stainless coat rack with 4 stainless steel hangers for my safety suits. Above the coat rack I mounted a pair of stainless steel baskets for racing shoes and gloves. On the ceiling I mounted a swiveling hook to hold my helmet.

Next to the overhead cabinets I mounted an Oil Rack and used Industrial Grey Velcro to hold the lift’s remote control in place. To the rear of the trailer is a strap holder, jack pouch, a blower holder and a couple cord holders.

I also put the hand tools in the appropriate drawers, but I’ll need to go back to clean and oil them before the first race.

In the attic I mounted a holder for four 5gallon fuel jugs.

I still have a day left to finish organizing myself into a 2′ shorter trailer.

Other

  • Installed an electric gate
  • Replaced all bulbs in Magnum XE with LED
  • Replaced AC blower motor on Magnum XE
  • Removed the Grill to the Magnum GT to paint when it gets warmer
  • Figured out I had the wrong parts to install an overdrive in the Magnum XE, and ordered the correct ones
  • Did a little cleaning and organizing in the shop

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SCREAMIN’ WOODY GETS NEW OIL PAN

I post this mainly in case someone had same issue as me.

Charlies Oil Pans had been making the fabricated oil pan to fit the Screamin’ Woody, my 60 Plymouth wagon. Charlies went out of business and when I contacted Stef’s, they said 2 months and $1000 to make one. Milodon made a off the shelf that. fits, but no windage tray for a 4.50″ stroke.

I found that 440 Source makes a pretty good looking 7-quart fabricated aluminum pan that fits, and there’s a windage tray for strokes up to.4.501″. It only cost about $225 for both and looks to be pretty high quality.

Hopefully the crank comes back from machine shop this week and engine can start to go back together. Need to cut a hole for the external oil pump and swinging pickup.

To The Track

With the Screamin’ Woody finally reassembled after a two year tear down from the Texas Whale and rebuild to the Screamin’ Woody, it was time to take it to the track. Normally I’d take it to San Antonio Raceway, a 1/4 Mile track about 200 miles away), but I was really Jonesing after missing Norwalk and Joliet, and the Indy race was coming up.

SHRA had an 1/8-Mile NSS Race in Denton (350 miles) on the 14th. While further and only 1/8 mile, it would help support NSS Racing (which is weak in the South) in Texas and give me competition practice. So I loaded up on Friday night and left for Denton early on Saturday morning. I arrived at the track at 1 pm, unloaded and got ready for the driver’s meeting at 3 pm. It was 98 degrees at 3 pm.

The wagon was in line to make its first hits since a total rebuild

First Qualifying was at 4 pm. I launched the car but it didn’t pick up the front wheels (like it use to) and carry the front end, but worst the that, the motor started to break up so I shifted. It quickly started to break up again – so I shifted again. It didn’t break up crossing the line, so I made a mental note that had to be in the 6000-6500 rpm range. Back in the pits, I only had time to cool the car down, put a charger on it, log the run, change tire pressure, and adjust the 5 point harness – which needed a foot taken out of the shoulder length.

First hit had a high 1.38 60′, and a 6.47@105mph

At 5 pm, just as I was finished with harness and we were called for last qualifying. I told myself that this pass I’d stare at the tach to figure out at what RPM it was breaking up. I dropped the slick’s pressure a 1/2 pound, launched at 2000 RPM, and starred at the tach. It started to breakup at 6300, and I shifted immediately. Again it broke up at 6300 and I shifted to third. I don’t have that time slip, but the 60′ improved slightly to low 1.38 and ET was 6.34.

Back at my pit, I got car ready for first round of Eliminations and did some Basic looking around to figure out why it was breaking up, and couldn’t see it. I had declared the 6.25 Index, and was hoping it might get cooler and I’d find the problem. It didn’t get cooler (95 degrees at 6 pm) and I didn’t find the problem – so I set my shift light at 6200 (normally 7200-7300 on a 572-13 head motor) and dropped the slicks another 1/2 pound psi.

Track photo from first round of Eliminations shows that not only is the car not picking up the front end well, it looks like a Chevy with the twisting

I was racing a slower car who would leave 3/4 second ahead of me. I was convinced that there was no way I could run the number (6.25), and would have to cut a great light for any chance. I got my wish with a .005 light, but my inexperience with the 1/8 mile stripe cost me when I took too much Stripe with a 6.248 ET on a 6.25 Index, or 2/1000 of a second too quick. My 60′ was a little better with a high 1.37. The car did not break up with me shifting at 6200.

2/1000 of a second too Quick

So I loaded up and was heading south by 7:30 pm, arriving back at the shop at 1 am Sunday. Other than the breaking up and launching with left front higher than right front, I was relatively happy with how the car performed, considering everything being new. On Monday, I backed the car out of the trailer, replaced the Distributor Cap and Rotor (both of which looked new), check all of my wiring to the plugs, and all wiring going to the MSD 7AL2 ignition box. I noticed that the box had 7000 rpm pills in it, and remembered reading that the pills (working by having their Ohms read and converted to a Maximum Limit of RPM allowed) can be off by as much as 10%, which 700 RPM, which subtracted from 7000 = 6300. I changed them out to 8000 RPM pills, which really should have been there in the first place. I put the car back in the trailer, and loaded spare parts consisting of a spare ignition box, spare distributor, spare set of plugs, and new set of wires.

Tuesday at 4 am I left my shop in Beasley, TX and arrived at my bud Doug Duell’s Mother’s house (Southern Indiana) at 6 pm. I dropped the truck and trailer there. Doug and Anne took me to dinner and put me up for the night. In the morning Doug took me to look at the new house that he’s building, and then to his dealership for me to look at the Palisades Limited, which I’m interested in a pair for Deb and I. At 9 am he took the lead with his motorhome and stacker, as I followed him in my dually and trailer. We had a little delay due to a Turbo issue on his coach. We got on the track at about 5, and I was at the hotel by 6.

Photo a NMCA Staff Photographer took and posted on their web site

I arrived at the track at 9 am, paid my entry, got car out of trailer, established credentials, got my chassis certified, teched the car in, and made it ready for the first 1/4 mile hit since being built. We checked the car’s timing, I charged up the dual 16v batteries, created a new weather station database for the car, and at about 1 pm (this is Thursday now) they called us for the first time trial. The car had an unimpressive 9.99 and 1.38 short time. Worse yet was that there was oil all over the front of the car, and another racer told me that I dropped a part at the line. I opened the hood and found the AN-12 Screw on plug for the oil filler was missing. I went to the starting line, and it was in the trash can, mangled an unusable. I couldn’t figure out how it could make six 360 degree turns and blow off – but it did. This would become understood later. I bought another fitting, screwed it on, and used electrical tape stretch around cap & bung to hold it on. I spent the next hour wiping the car down underneath of all of the oil. When called for next time trial, and after my burnout – I was backed up and off the track with them saying I was leaking oil.

I went back to the pits and spent three hours under the car wiping up oil and trying to figure out where three mystery leaks were coming from. I finally got under the car with it running and only then did I see weeping from the oil pan gasket — which the engine builder had used grey Permatex to make. Many of the oil pan nuts were loose – and I snugged them down. Just as I was lowering the car — the track announced a clean up session for those who didn’t get two test hits — and I hustled off to it.

After I came out out of the burnout area I had all of the track people looking under the car for any drip. They cleared me and I pre-staged, Staged and took off. All was going well until the 1000′ when I looked in the mirror just as the car started smoking. I immediately pulled over and off the track’s first exit. Off the track I found I was leaking oil all around the oil pan. It was late and I was both worn out from working all day in the heat and sore to where my back and shoulder were killing me. I was going to throw in the towel for the day and try to deal with it in the morning — but Jeff Frees talked me into dealing with it that night.

Doug Duell was the only one small enough to drive the car onto the lift in Jeff’s trailer

Long story short, Doug Duell drove the car onto Jeff’s lift, Jeff and his crew started to tear the car apart, I drove to an all night auto parts store in Indianapolis for a couple of gaskets, and I was back at the motel by midnight. I was back at the track at 6:30 the next morning to clean up the car and make ready for the First Qualifying at 8:30 AM. I took it for a ride to blow off any extra oil that I might have missed off the car, and gave it a final check. All looked good.

So they call us for the first qualifying hit — and that’s when we noticed that oil was under the car again. Again to make a long story short, my vacuum gauge in the car wasn’t working and Jeff came over with a manual vacuum gauge to take a reading and adjust in more vacuum to slow the leak, so I could make the pass. That’s when we got the puzzling gauge reading of positive pressure instead of vacuum. It was too late to make a hit — so I got out of my racing suit and headed over to the car to disconnect the vacuum pump for Q2. While Brent Wheeler and I were looking at what was needed to disconnect — we both, at the same time, realized the hoses had been installed backwards. While both hoses were the wrong length to be properly swapped around — they did fit for a temporary fix. I did that and made it in time for the second Qualifying — which appeared to be good — albeit slower than expected.

Track photo of Screamin’ Woody’s Pass in Second Qualifying Round

The next round was the first round of class eliminations for FX. There was a couple grand on the line — including $1600 in side bets to the winner. I was matched up against Dan Cook, who was the faster car by 1/4 second. Car felt good on that pass, and I saw the Win Light for me – but when I picked up the time slip I found that I’d run a 9.9 on a 9.75 Index and only won because Dan had a really bad light. Worst yet, after I picked up the ticket — I started hearing a noise that sounded like valve train clatter. I still had oil pressure but the motor didn’t sound right. In the pits, dozen’s of people were coming by to give their opinion and advice. After the valve covers came off and on three times — I was done and parked the car in the trailer.

I returned to the track the next day to be a spectator and attend that evening’s Dave Duell Classic Dinner. I left the track at about 10 pm with my truck and trailer, got a little sleep and left the motel at 4 am. I arrived at my shop (1125 miles later) at 11 pm.

In the shop, we first thought that the noise was from a couple of rockers rubbing on the valve cover. The valve covers were clearanced and we still could hear the noise/ With a stethoscope it sounded like it was coming from under the valley pan – lifters suspected. When the lid to the valve cover was removed, it was noticed that pools of race gas had formed in the damned off areas. A witness mark showed that the levels were as high as 3/4″ before draining through the bolts holes into the motor. Draining the oil found a lot of gas in the oil, which only had two runs on it. A shop rag dipped into the oil more closely exploded than burned when a match was put to it. It was decided to pull the motor. There are some issues. A puzzling one is that the rods and crank bearing surfaces appear to have been contaminated and have specs on them. We’re assuming from the race gas. So that’s where we’re at with the wagon as I write this.

Screamin’ Woody Goes To The Track

Finish Interior

The door cards on the Texas Whale were cardboard with black and gray carpet glued on. For The Screamin’ Woody, I wanted to match the red exterior a little more – so the seats were dyed red, the cage painted gold hammered, a red window net and safety harness installed – and I wanted the door panels in a red quit pattern. I made the door cards out 1/8″ plywood, drilled the holes for door handle and mounting screws, and pulled some vinyl quilted fabric I bought on Ebay.

Get Ready To Race

I’d taken the car for a couple of blasts on the rough (from farm tractors running up and down it all day, everyday) 35 mph narrow road that the shop is on, and made adjustments between blasts. The problem is you can only conduct your testing to about 3/4 of the cars capability, because of the terrible condition of the road. I wanted to take the car to race at the NMCA Nationals in Indy this coming weekend, but needed to take to a more local track this past weekend, to see if it was worthy to take to Indy.

SHRA had an 1/8 mile race in Denton (350 miles from the shop) yesterday, and I decided to take it there. While cleaning the car up, I noticed a lot of overspray on the front fenders and doors, from when it was painted under the hood. That took me better than 4 hours of slow clay-barring to get right. Then I loaded it into my trailer.

Racing In Denton

Friday the 13th, I loaded up the truck and trailer with what I needed to race. At 8am Saturday I left for the 350 mile drive to Sanger, TX. I arrived on the track at 1PM to say my Howdies, unload car and set up my pit. At 3PM we had our Driver’s Meeting and at 4PM we had our first Qualifying run – in 97 degree heat.

ON the first pass I had a decent .043 light (considering it was June since I last took a stab at the tree) but the car started to break up way before the Shift-Light was suppose to come on – so I made my 1st-2nd and 2nd-3rd shift as soon as I felt it break up. Frankly, I was busy mentally monitoring my concerns of going down the track in a car that had every nut and bolt removed, every component rebuilt or replaced, and reassembled. Other than the breaking up at higher RPMs, the car felt good – but I was unable to look at the tach to see where it was breaking up. I was guessing it was about 6000 RPM as I wasn’t breaking up crossing the Stripe.

My Safety Harness was all screwed up, as I forgot to adjust the length when new ones were installed so I spent much of the half hour between the First and Last Qualifying fixing that. I was able to verify that the Fuel Pressure was right at 8psi and make a shock and tire adjustment to try for a better 60′. I told myself that I would stare at the tach to figure where it broke up. The sun was in front of the tree and I totally missed the lights, but was able to improve my anticipating the breakup and shift quicker. I was able to find that the breaking up was occurring around 6300-6400 RPM.

I decided that as opposed to weighing the car down for the 6.41 Index, that I’d shoot for the 6.25 Index by setting my shift light for 6200 (before the breaking up), as opposed to closer to the 7500 RPM that those heads (572), Cam and 2 1/2″ headers wants. I figured that and the weather getting cooler might give me the .06 I needed. When they called us to race, it was still 94.5 degrees and I felt I would have a hard time hitting 9.25, so I’d need a killer light. I also took 2 more Clicks out of the front shocks. I had to line up against Gary Durham, who had a slower car, so he’d leave first. The setting sun still had the tree right in the middle of it, concerning me about seeing the light and pushing the Tree. Gary left, and I left. I felt I had a decent light as I was going down the track. As I was coming to the stripe and passing Gary, he jammed the brakes and gave me the Stripe. When I picked up the ticket it was the yellow copy, meaning loser! Looking at the ticket I saw I threw away a .005 reaction time by running a 6.2477 on a 6.25 index. 23/1000 of a second too fast.

So I was loaded and on the road by 7:00 and home by 1AM

Getting Ready For the Nats at Indy

Tomorrow I’ll back the car out of the trailer; make a floor modification to the trailer; and change the distributor cap, rotor, ignition chips, and wires on the Wagon. Give the car a quick Cleanup and load it up again. I’ll track down some parts like a spare regulator, distributor and plugs, and take the fuel pump and carbs off the Thug to bring to Indy – and I’ll try to fix the car at the track. I leave at 4am Tuesday.